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View Full Version : Z-grip RT Classic - rebuilt!



Pghp8ntballer
01-10-2016, 05:17 PM
First a pic. Picked it up over on MCB. Unfortunately the grip has holes drilled in it :( One is clearly for adjusting the rear trigger stop. The other holes which are about 1/4" or so below the other are for nothing? I do not have a pic yet.

http://i1105.photobucket.com/albums/h347/pghp8ntballer/Automag/image_3.jpeg (http://s1105.photobucket.com/user/pghp8ntballer/media/Automag/image_3.jpeg.html)

Now the questions.

First off, it cycles fine but leaks out the back. The air comes through the velocity adjuster hole in the back. It slowly fades away with the trigger pulled. I put a new Oring on the reg piston in the back half, but it did not change. Yes, I ran oil through it to see if it went away. It didn't.

Secondly, to adjust the reactivity of the valve, do I grind the fat end or thin end of the on/off pin? No I am not buying an SHP tank under any circumstances. Currently, my pin is at .740" length.


**Update**
The leak out the back was a damaged reg piston Oring. I put a new one on again and got the same result. I inspected the internal body where the reg piston goes and sure enough there is a bad gouge in it.

What are my options?
-Replace the valve assembly? I don't want to buy a whole new valve. It's way more than I want to put into this gun.
-Is there any reason I can't just find a classic RT valve body back and swap it on? Does anyone have one? -Is there any chance the gouge could be repaired? My thoughts are no?

Thanks!

Nobody
01-10-2016, 05:40 PM
It does not take much to shorten the pin. Its best to use a digital set of calipers and try to take off only .005 at a time if you can. That way you can tailor the reactiveness with the tank. Shorten the smaller end of the pin.

captian pinky
01-10-2016, 06:25 PM
your pin should be about right. I would just oil your mag regularly and it will begin to rt.

Pghp8ntballer
01-10-2016, 06:28 PM
I already have the digital calipers. Thanks for the info!

athomas
01-10-2016, 06:44 PM
A leak out the back is quite possibly the regulator seat oring. If you have a level 10 bolt, the regulator piston assembly needs to be the newer higher pressure version as well.

You can simulate a shorter pin by inserting a couple of ULT or level 10 shims in between the on-off assembly halves. It prevents you from having to alter your pin.

Pghp8ntballer
01-10-2016, 07:24 PM
I do need to order a complete set of Orings for it though...

Yes it does have L10 but how do I tell what regulator piston assembly I have? I will keep the shim note in my mind.

Cyco-Dude
01-11-2016, 02:18 AM
increasing the tanks output pressure is the correct way to do it. that pin is already starting to get short. also, take care if you have an original rt sear. the carbide inserts may be hard, but that also means they are brittle and prone to chipping.


I do need to order a complete set of Orings for it though...

Yes it does have L10 but how do I tell what regulator piston assembly I have? I will keep the shim note in my mind.
do you have any o-rings for it at all? the lvl 10 o-ring is the same size as the reg seat o-ring, so if you have a spare one of those you can use that. there could also be some debris in there causing it to leak. if you don't have any o-rings at all, i would just get a parts kit (probably go with an rt classic; as that one has replacement banjo bolt o-rings and a couple of reg seat o-rings; one of which you could keep as a spare for the lvl 10).

Pghp8ntballer
01-11-2016, 06:40 AM
I don't recall seeing any carbide on the sear. I didn't know they made them differently. But no signs of wear. I made sure to check when I tore it all down and cleaned everything. This is my first non-classic valved mag.

I did put a new urethane Oring on the reg piston and one or two on the on/off but that's all I had spare wise. I might have an L10 Oring though. I'll have to check. I am going to order a parts kit this evening after work.

When I cleaned it, there was some debris in the spring stack. I also found an entire Oring like a tank Oring, smashed under the reg piston. So I could have some more stuff in there.

Pghp8ntballer
01-11-2016, 08:01 PM
I found the leak. The brand new reg piston Oring had a big chunk taken out of it. I put a new one in, and immediately had the same issue. There is a knick or burr in the rear valve body itself that is causing the Oring damage.

What can I do about this?

Spider-TW
01-12-2016, 10:31 AM
I found the leak. The brand new reg piston Oring had a big chunk taken out of it. I put a new one in, and immediately had the same issue. There is a knick or burr in the rear valve body itself that is causing the Oring damage.

What can I do about this?

If the gouge only cuts the o-ring during installation and is not in the running area of the o-ring, you can burnish and sand it out. It could be from the spring rubbing on the body (which is not a seal area), so you would grind that edge off of the spring as well. If it's in the seal area, that would be tricky.

luke
01-12-2016, 10:35 AM
There is a knick or burr in the rear valve body itself that is causing the Oring damage.

Can you post a clear, in focus, close up picture of the burr?

Pghp8ntballer
01-12-2016, 10:49 AM
I will try. My photographing black items is poor.

It's actually more of a gouge. I will check the spring for potential issues causing the gouge. It does seem to be high enough that it should not be in the seal area. But on the first air up, it cycled great for about 20 shots then it started to leak. With the second Oring, it was damaged immediately. The reg piston looks fine.

Pghp8ntballer
01-12-2016, 11:41 AM
Here are the pics. On further inspection, i really don't see any burrs or gouges. It appears I was looking at the pressure relief port? The hole goes all the way through. But it looks like there is epoxy or something mostly blocking the hole. It does not feel significantly rough on the inside where the piston goes. Also, there are a couple other pictures trying to show no other obvious damage to the body. Other pics show the reg piston and damaged oring. Both orings that were damaged looked like they were damaged identically or awfully similar. No signs of roughness on the reg piston itself. The inner reg spring is rough on the ground edges which I will smooth out just in case. No offending debris was found. But now I am not entirely sure what could cause the oring damage.

http://i1105.photobucket.com/albums/h347/pghp8ntballer/DSCN3895.jpg (http://s1105.photobucket.com/user/pghp8ntballer/media/DSCN3895.jpg.html)

http://i1105.photobucket.com/albums/h347/pghp8ntballer/DSCN3902.jpg (http://s1105.photobucket.com/user/pghp8ntballer/media/DSCN3902.jpg.html)

http://i1105.photobucket.com/albums/h347/pghp8ntballer/DSCN3899.jpg (http://s1105.photobucket.com/user/pghp8ntballer/media/DSCN3899.jpg.html)

http://i1105.photobucket.com/albums/h347/pghp8ntballer/DSCN3903.jpg (http://s1105.photobucket.com/user/pghp8ntballer/media/DSCN3903.jpg.html)

http://i1105.photobucket.com/albums/h347/pghp8ntballer/DSCN3905.jpg (http://s1105.photobucket.com/user/pghp8ntballer/media/DSCN3905.jpg.html)

http://i1105.photobucket.com/albums/h347/pghp8ntballer/DSCN3904.jpg (http://s1105.photobucket.com/user/pghp8ntballer/media/DSCN3904.jpg.html)

Thoughts?

Spider-TW
01-12-2016, 12:19 PM
That should be a urethane o-ring, probably 90 duro. However, I suspect Athomas was correct about the reg seat leak, which would overpressure the piston, pushing it back to the vent, where the o-ring extrudes into the hole. When you fire, the piston drops and chops the edge off of the o-ring.

That would also explain the bits of o-ring you found.

I forgot that the reg spring doesn't even run in the same bore as the seal.

Pghp8ntballer
01-12-2016, 12:52 PM
That is a urethane Oring... But 70D. Thanks for the elaboration on what Athomas said. It makes sense. Still new to these regs.

Everyone else agree with this? So just give her a full rebuild and we should be ready to go?

Athomas mentioned an updated reg piston assembly for use with the L10. Judging by my pics, do I have the correct part?

So what is the best way to adjust the RT effect? File the pin, or add ult shims between the on/off halves? I will be placing an order with Tunaman, so I want to make sure I get everything in one order.

I greatly appreciate all the wisdom guys!

athomas
01-12-2016, 04:23 PM
That is a urethane oring? It looks quite dark in the pictures. I would have guessed it was a buna oring as well. Try a harder 90 durometer urethane oring to see if it helps.

You can't tell if its an updated reg piston assembly. If it doesn't leak out the back when you are shooting at the desired velocity using a red or grey bolt spring, then it is probably an updated piston assembly. If it doesn't leak out the back at really low velocities or at a setting that won't allow the gun to shoot, but starts to leak as you increase the velocity, then it is probably an older assembly.

The shims in between the halves will allow you to experiment with reactivity without filing down your pin. Since you have a shorter 0.740" pin, you shouldn't need to file it down if you use the shims. Don't use too many shims. Too many shims will cause the top to squeeze the oring on the pin and reduce your reactivity. If you have to press the on-off assembly into the valve with quite a bit of force in order to get the valve into the body, then you have too many shims installed. If the on-off assembly fits nicely and the valve slides into the body without restriction, then you are fine.

Pghp8ntballer
01-12-2016, 04:32 PM
Yes, it is definitely urethane. I bought a standard set of 10 each from mcmaster carr. They are all black, not the expected clear.

Are the ULT and L10 shims the same? So simply unscrew the two halves of the on/off, put in a shim at a time and reassemble?

Once I get the gun up and running, I will tune for the RT.

The only other odd situation I had was when I first aired it up and did not leak, It was shooting 350 fps or so (with a chrono). I turned it out quite a bit but it never dropped. After about 20 cycles/shots or so it started the leak. It has the gold mainspring on the bolt.

athomas
01-12-2016, 05:23 PM
ULT shims are 0.005" thick and level 10 shims are 0.010" thick. Two ULT shims equals one level 10 shim. Yes, just unscrew the two halves and put a shim over the threads and reassemble.

If you aired it up and couldn't get it to shoot under 350 fps, even after turning the adjuster out quite a bit, its most likely that your regulator seat oring is leaking.

Pghp8ntballer
01-12-2016, 05:25 PM
So that just reiterates your initial thoughts. Even better. ULT and L10 shims are the same ID and OD then?


Why does the regulator piston in my valve look completely different than the AGD blow-up diagram of the retro valve and in the parts break down?

luke
01-12-2016, 05:27 PM
The type of damage to the oring looks to me like it's getting clipped off as it's being compressed to squeeze into the cavity. I would chalk this up to being the wrong o-ring and or material type. I have seen that exact damage to o-rings in the prototype stage of making and designing parts. Generally it has to do with the wrong parameter spec for the o-ring being used, for example stretch, compression, groove size and cavity diameter. Since we know the AGD parts are to spec I would bet that the spec of the o-ring is incorrect including the material type.

Pghp8ntballer
01-12-2016, 05:34 PM
Hmm. Its a 70D 012 urethane oring. Good to know.

Luke, Athomas, anyone else... should I purchase a new reg piston while I am at it? Or should I use the one I have?

So my parts list to order are...

genuine AGD RT parts kit
L10 rebuild orings
RT pin (to have as a spare)
one pack of ULT shims
Spare bolt foamie
new reg piston???

luke
01-12-2016, 05:49 PM
Its a 70D 012 urethane oring.

I'm simply saying that I've seen that exact damage and it was due to in correct specifications. The "odd part out" here is the non AGD spec o-ring so if there is no visual damage to the piston or cavity the first thing I would do is install the correct o-ring. I do suggest that you remove the o-ring and closely inspect the parts under a magnifying glass to see if there is any damage. I would only replace the piston if it's damaged beyond repair. If there is a burr or something, that can probably be repaired...

Pghp8ntballer
01-12-2016, 05:59 PM
Understood. I used the urethane over buna to prevent a possible issue. But I will order the genuine agd kit. Unfortunately I do not have a magnifying glass.

luke
01-12-2016, 06:04 PM
I have always had a magnifying glass in my gear bag, found many damaged o-rings. I even inspect the new ones before and after installing them. ;)
http://www.ebay.com/itm/Loupe-Doublet-Chrome-GLASS-LENS-10X18mm-Lupe-Loop-Pawn-Shop-Jeweler-Gold-Diamond-/111857444051?hash=item1a0b3924d3:g:86UAAOSwnipWU5q ~

Spider-TW
01-12-2016, 06:21 PM
Off spec or not, the o-ring shouldn't normally reach the vent to get nibbled upon.

You can use non-AGD o-rings as long as they are the right size and material. I bought a bunch of good banjo bolt o-rings from mcmaster, then got my RT to stop chewing them. :rolleyes:

Avoid Chinese o-rings. I've seen some absolutely terrible round things they sold as o-rings. That was one of WDPs A1 angel problems; the Chinese o-rings were bad out of the box. I have one where I had to replace most of the o-rings just to get it running the first time, brand new.

Pghp8ntballer
01-12-2016, 06:32 PM
I noticed the el-cheapo orings I have from Harbor freight are clearly not the correct size. I was able to put new banjo bolt orings on since I had ordered a 100 pack or 90D buna 009 and other sizes from McMaster Carr a while back. Their orings are usually pretty good. I only have like 90 more of those 90D orings for the banjo bolt. They were so hard to put on due to the duro, I doubt I will need the other 90 I have, lol.

luke
01-12-2016, 06:35 PM
If you have a level 10 bolt, the regulator piston assembly needs to be the newer higher pressure version as well.

Re-tuned not replaced. ;)

Pghp8ntballer
01-12-2016, 06:37 PM
cool beans there!

luke
01-12-2016, 06:38 PM
Off spec or not, the o-ring shouldn't normally reach the vent to get nibbled upon.

I would wager it's getting clipped on the leading edge of the cavity during install not the vent hole.

athomas
01-12-2016, 10:53 PM
Re-tuned not replaced. ;)
Yes, but most don't have the ability to retune them like you or a few others here.:)

I agree that the oring is probably getting pinched on the install into the cavity, or is getting pinched in the groove once the pressure hits it if it is the wrong spec (ie; too loose or wrong dimensions).

Cyco-Dude
01-13-2016, 02:16 AM
um...someone did tell you that that isn't the correct piston right? that's an old version piston for an automag classic valve. the piston you want is this (http://store.airgundesignsusa.com/index.cfm?fuseaction=product.prodInfo&prodId=1869).

come on guys; he has an rt classic. you all should've picked this up right off the bat.

Pghp8ntballer
01-13-2016, 06:25 AM
I asked bout that twice. Outright saying it does not look like the one in the blow up diagrams.

Cyco-Dude
01-13-2016, 08:37 AM
I asked bout that twice. Outright saying it does not look like the one in the blow up diagrams.
lol, they were too busy talking about the o-ring to notice it was the wrong part i guess! :p

vintage
01-13-2016, 07:01 PM
i never opened the pics at work since so many people were helping.:D

athomas
01-13-2016, 09:53 PM
:tard: I was so fixated on the oring, that I didn't even look at the piston assembly. Ha ha. That'll cause a problem for sure.

Spider-TW
01-14-2016, 04:07 PM
I didn't think a non-RT piston would fit in there and work for any amount. I thought I just didn't remember what the classic RT piston looked like. It was weird, but I just didn't believe it. That's worse than my friend asking me to tune his minimag that was missing the whole on/off top assembly.

Pghp8ntballer
01-14-2016, 07:41 PM
It happens. I was able to get the piston ordered with the other parts and not get double tapped on shipping so no harm done. Oddly enough, it seems to be the perfect size for the classic valve piston as well. Its not too tight and not too loose.

ChristianFromPitt
01-15-2016, 10:09 AM
I'm always impressed at this community. It's like a bunch of mag detectives working together with a lot of expert eyes that can spot things I wouldn't notice.

Pghp8ntballer
01-24-2016, 05:00 PM
I am a little late with the update. I got my parts in earlier this week and was able to rebuild it. All new orings throughout sans L10 and the new reg piston. I only had larger carriers for the L10 so the new L10 stem orings leaked with the ones I had. I ended up just replacing the carrier exterior boring and leaving the L10 as-is since it did not leak to begin with. It shoots and chrono's fine.

However... I am noticing bolt stick/reseting issues. I have tried cranking the thumbscrew down and various states of tightness. Snugged good with an allen wrench seems the most reliable. The issue is not always occurring but its like the air is choked off and there is a lack of a trigger. If I push the bolt back with a dowel, the trigger resets. Could the new orings in the on/off need broken in? Could the front screw need tweaked? I also thought I might be getting choked off at tank reg but I tried 2 different PE 3k tanks and my armageddon system. I did notice that it seemed vaguely more reliable at a higher output. *NOTE* I am outright against pumping high pressure into a marker. 900psi had it shooting decently. I tried up to 1100 but it did not make a difference... even in the RT department. I tried 3 different mainsprings too. The one that came with the gun, the new L7 RT spring that came with the new rebuild, and a red L10 spring. It felt like it was causing lighter or stiffer trigger pulls. Does that make sense? It did have a bit of an effect on the sound signature and feel of the marker as well as varying effects on the antichop (All of this testing was done dry firing). But I was still getting the issue with all the springs.

Onto the RT tuning. Since I took it up to 1100psi with no avail, I decided to file the pin down. The original length was .740" I did try the ULT shims. Any more than two and the on/off was too thick to sit flush and it didn't seem to have an effect. To the file I went. I filed about .005" to .007" or so off at a time and retested. I couldn't shoot much since the armageddon is set up on a 17ci 3k tank. At .724", I started to feel the RT coming about. It was feeling better, but still slow. My goal is about a 10-15 bps RT. I went a little further with the pin. I am down to .719" at 900 psi but I ran out of air on the little tank. I guess I will have to set the Armageddon up on a bigger tank since it seems to run the best at 900 psi So... to be continued.

Does any of this make sense to you?

athomas
01-24-2016, 07:15 PM
However... I am noticing bolt stick/reseting issues. .... If I push the bolt back with a dowel, the trigger resets. Could the new orings in the on/off need broken in? Gnerally, if the trigger resets when you push the bolt back, then the issue is powertube related. It is usually a bolt stick issue caused by a carrier oring that is too tight.

Check the body washer to see if the hole is mushroomed. A mushroomed hole could cause the bolt to rub, adding to the friction which would require more force to reset the bolt.

Pghp8ntballer
01-24-2016, 08:24 PM
I will look into the body washer. But do the stainless bodies have the washers? I thought that was for the aluminum bodies?

Carrier oring... the white one that the bolt stem goes through or the black exterior carrier oring?

I work late this week so I may not get a chance to tinker with it until the weekend.

Cyco-Dude
01-24-2016, 09:04 PM
I am a little late with the update. I got my parts in earlier this week and was able to rebuild it. All new orings throughout sans L10 and the new reg piston. I only had larger carriers for the L10 so the new L10 stem orings leaked with the ones I had. I ended up just replacing the carrier exterior boring and leaving the L10 as-is since it did not leak to begin with. It shoots and chrono's fine.

However... I am noticing bolt stick/reseting issues. I have tried cranking the thumbscrew down and various states of tightness. Snugged good with an allen wrench seems the most reliable. The issue is not always occurring but its like the air is choked off and there is a lack of a trigger. If I push the bolt back with a dowel, the trigger resets. Could the new orings in the on/off need broken in? Could the front screw need tweaked? I also thought I might be getting choked off at tank reg but I tried 2 different PE 3k tanks and my armageddon system. I did notice that it seemed vaguely more reliable at a higher output. *NOTE* I am outright against pumping high pressure into a marker. 900psi had it shooting decently. I tried up to 1100 but it did not make a difference... even in the RT department. I tried 3 different mainsprings too. The one that came with the gun, the new L7 RT spring that came with the new rebuild, and a red L10 spring. It felt like it was causing lighter or stiffer trigger pulls. Does that make sense? It did have a bit of an effect on the sound signature and feel of the marker as well as varying effects on the antichop (All of this testing was done dry firing). But I was still getting the issue with all the springs.

Onto the RT tuning. Since I took it up to 1100psi with no avail, I decided to file the pin down. The original length was .740" I did try the ULT shims. Any more than two and the on/off was too thick to sit flush and it didn't seem to have an effect. To the file I went. I filed about .005" to .007" or so off at a time and retested. I couldn't shoot much since the armageddon is set up on a 17ci 3k tank. At .724", I started to feel the RT coming about. It was feeling better, but still slow. My goal is about a 10-15 bps RT. I went a little further with the pin. I am down to .719" at 900 psi but I ran out of air on the little tank. I guess I will have to set the Armageddon up on a bigger tank since it seems to run the best at 900 psi So... to be continued.

Does any of this make sense to you?
the z-grip is not the best for rt'ing in my experience. the stock carbon grip or a modified intelliframe would be best. as for the pin, frankly i think that way beyond spec. you might try a .712 pin with a quad o-ring (that's what is used in an emag) and see if that helps. beyond that, i think either get a different frame or a different gun, or otherwise just use it as-is until the o-rings break in. i don't think continuing to alter the pin will be good in the long run, but it's your gun...

athomas
01-24-2016, 11:08 PM
The body washer in the stainless bodies, is the washer that is welded in place between the valve and the breach area.

The carrier oring is the white one that you are adjusting with the carriers. The black ones on the outside of the carriers rarely need replacing and never cause issues unless you actually break them.

Pghp8ntballer
01-29-2016, 09:09 PM
Got to try some troubleshooting this evening. I aired it up and set to 900psi as before. This is with the pin at .719". It cycled the same, but the brief RT effect seemed closer to what I wanted. The bolt stick still seems prevalent. Off the top of my head, the trigger rod gap was about the thickness of 3 credit cards. I shortened it to about a single credit card thickness. It seemed to cycle a lot better but still plagued by bolt stick. The RT effect felt spot on for the speed I want and lasted a bit longer. It's still tricky to get it to RT. Oddly enough, if I do not try to RT and just fan ( I think that is the right term for it) the crap out of it, it shoots good. Single or slower shots sometimes stick. Throughout this I did turn it down to 800psi and got essentially the same results except the RT was not as quick/easy to attain.

I took a peek down both ends of the body. I don't see any damage or mushrooming of any kind. I will have to try the next size up carrier.

My Armageddon tank valve also sprung a leak during troubleshooting :(

athomas
01-29-2016, 09:32 PM
The RT effect depends on the sear cycling quickly. If you are getting bolt stick, it will affect the ability to RT. Get the bolt stick issue fixed, and your RT effect will probably be fine, or at least be much easier to adjust.

Pghp8ntballer
01-30-2016, 08:05 AM
As per your previous post, try the next size up l10 carrier?

Pghp8ntballer
01-30-2016, 04:37 PM
Ok, more troubleshooting. I tried the next size up carrier. Leaks like a sieve. Too loose. I tried 4 different new-from Tunaman white carrier Orings in the second smallest carrier... The one with just a dot on it. All leak badly or won't even hold the bolt in place when inverted. I then tried the L10 kit from my classic smart mag. A bit of leaking and short stroking but seems to not have bolt stick issues. I think that L10 kit may need a rebuild. I do not have the smallest carrier. But after tearing the smart mag L10 kit back out of th RT, I noticed that the bolt stem of the Kit that came with the RT was backing out! What are the chances that I run across 2 bolt stems backing out on 2 different guns in a 6 month timeframe?

http://i1105.photobucket.com/albums/h347/pghp8ntballer/Automag/image_5.jpeg (http://s1105.photobucket.com/user/pghp8ntballer/media/Automag/image_5.jpeg.html)

:banghead:

To be continued...

Spider-TW
02-05-2016, 01:05 PM
Besides that level 10 stem which is a problem, are those 90 duro o-rings on the banjo bolt? 70 duro are not a good idea there when it comes to getting a bolt to behave.

vintage
02-06-2016, 10:49 AM
I would be willing to bet most of your problems are the bolt stem on the level 10, they are a friction pressed fit and have been know to come loose. as for the rt effect I have 6 rt classics and the effect is different on all of them off the same tank.

Pghp8ntballer
02-06-2016, 12:41 PM
Yes the banjo orings are all 90 duro.

The bolt should be arriving at AGD today or Monday for replacement.