LittMag
09-28-2002, 09:06 PM
First off I want to thank the people at EMR who tried to help me with my mag (Rich on team Joint Fury and Shag from that grey bus)
I have a
Classic Mag
Intelliframe
running on a fixed 850 psi off crossfire stub
The marker will charge up, but it will not fire. The marker was recently purchased used, with a serial number 406** it has one star, but what's odd is that it has a removeable powertube.
These are the things that I have checked:
1. Trigger rod, adjusted to ~1/16 of an inch from the trigger
2. Checked the body to make sure the body was to the correct tollerances (it's one of those electroplated black ones) I replaced the body with a classic feed grey one.
3. Spring pack was dry so I put some white lithium grease on it (suggested by mag users at castle conquest)
4. on/off pin is being fully depressed, I removed the trigger grip and physically pushed the sear back to make sure of this
5. bolt is back against the bumper when the marker is charged
Possible things that could be wrong, but I'm not too sure so any suggestions are appreciated as to how I can fix, else I will send into AGD for repairs.
1. Valve is just plain messed up, b/c it's the wrong level
2. Bolt could be being pushed at a slight downward angle so that it is being stopped on the washer welded into the body.
3. Perhaps the on-off pin was shortened, but I have no idea.
Anyone have any ideas? I think I've run through the gambit of things I can check but who knows I could've missed something.
I have a
Classic Mag
Intelliframe
running on a fixed 850 psi off crossfire stub
The marker will charge up, but it will not fire. The marker was recently purchased used, with a serial number 406** it has one star, but what's odd is that it has a removeable powertube.
These are the things that I have checked:
1. Trigger rod, adjusted to ~1/16 of an inch from the trigger
2. Checked the body to make sure the body was to the correct tollerances (it's one of those electroplated black ones) I replaced the body with a classic feed grey one.
3. Spring pack was dry so I put some white lithium grease on it (suggested by mag users at castle conquest)
4. on/off pin is being fully depressed, I removed the trigger grip and physically pushed the sear back to make sure of this
5. bolt is back against the bumper when the marker is charged
Possible things that could be wrong, but I'm not too sure so any suggestions are appreciated as to how I can fix, else I will send into AGD for repairs.
1. Valve is just plain messed up, b/c it's the wrong level
2. Bolt could be being pushed at a slight downward angle so that it is being stopped on the washer welded into the body.
3. Perhaps the on-off pin was shortened, but I have no idea.
Anyone have any ideas? I think I've run through the gambit of things I can check but who knows I could've missed something.