Lvl 10 Bolt Rushing forward and not returning

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  • gunangel
    AGD Pride
    • May 2005
    • 285

    #16
    sorry to jump in, but same thing is happening to mine. worked fine then suddenly i gas it up, it rushes forward and stays that way. putting a squeegee down the barrel will not let the bolt reset. I was running no shims for a while and that fixed it, then it did the same thing and running two shims fixed it for a while, then it did it again. I tried switching out carriers and all but the same thing is happening. backed out my detents and I'm essentially in the same boat as warbeak.

    switching valves fixed the problem but if possible I'd like to save my X...
    BTW I'm running a Lvl X and ULT.

    I have 3.5k left in my tank and I switched to a harder spring and put in an RT on/off and ran oil down the asa...unfortunately it's 11pm so I'll have to try it tomorrow, but any other recommendations?

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    • warbeak2099
      That is my foot!
      • Jan 2004
      • 4447

      #17
      Originally posted by michbich
      If you drop in another valve, does it still do the same thing?

      If it has done this on 2 different valves with 2 different sears. Was it in 2 different bodies/rails as well?
      I've tried the same valve in two different Mags. One Mag has a classic rail and sear, and the other has an RTP rail and sear.

      Sticking a squeegee in front of the bolt does nothing. The bolt simply fights to move forward against the squeegee.

      I also tried a stiffer spring.

      It seems as though the sear is not catching the bolt. This would mean the bolt is worn since two different sears (in great condition) have failed to catch it. I cannot see any signs of wear on the bolt though. The bolt lip looks immaculate.

      Perhaps it is a problem with the ULT. It's as if the ULT isn't pushing down hard enough on the back of the sear to push the front of the sear up to catch the bolt.
      Last edited by warbeak2099; 10-06-2008, 06:43 AM.
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      • BigEvil
        www.BigEvilOnline.com

        • Feb 2005
        • 9333

        #18
        Try another bolt on that valve and see what it does.

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        • michbich
          machinist-biochemist
          • Jul 2007
          • 849

          #19
          Maybe the bolt is out of tolerance or is not concentric. What happens is you hold down the trigger? Does it reset?

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          • secretweaponevan
            Only HALF Polish!
            • Sep 2007
            • 1132

            #20
            If you hold the trigger and the bolt stays in a forward position and air is leaking out, you have an on/off problem.

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            • Coralis
              Hyper Micro
              • Aug 2005
              • 1285

              #21
              Try pulling the ult apart perhaps the pin snapped, bent or came unscrewed.

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              • gunangel
                AGD Pride
                • May 2005
                • 285

                #22
                it looks like we have the exact same problem.

                pushing against the bolt does pretty much nothing as the bolt continually fights to move forward. (no click of the sear catching etc)

                the valve is leaking down the barrel with or without the trigger held. (sound does not change)

                pulling the trigger pretty much doesn't seem like it does anything as the valve will continue to leak.

                the bolt seems to be without wear and tear. then again I don't have another Lvl 10 bolt to try this against.

                checked the ULT it looks perfectly fine...although I have 10 shims in it...but then again it worked with this setup a short while ago so that shouldn't be the problem.

                the thing is at least for me it worked, then it didn't, then it did, then it didn't again, so the bolt being out of round seems strange. I'll try eliminating the ULT and see how that goes.

                I'm really in for more ideas!

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                • secretweaponevan
                  Only HALF Polish!
                  • Sep 2007
                  • 1132

                  #23
                  Originally posted by gunangel
                  pulling the trigger pretty much doesn't seem like it does anything as the valve will continue to leak.
                  You have a leak in your on/off. Start there.

                  I'd remove most of those shims and start over.

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                  • secretweaponevan
                    Only HALF Polish!
                    • Sep 2007
                    • 1132

                    #24
                    Originally posted by warbeak2099
                    Alright I'm at my wit's end. I've over shimmed and undershimmed the powertube and no matter how many shims I have in there, the bolt just rushes forwards and vents air when I gas up the gun. There is no wear on the sear or bolt lip. Diagnosis?
                    Your sear isn't engaging the bolt.
                    This could be because:
                    your on/off pin won't go up for some reason
                    your on/off has a leaky o-ring (test for this by holding the trigger when you gas up)
                    your sear is cracked near the pivot hole
                    your trigger rod is too long
                    your sear is hung up
                    you are missing the rail bushing

                    You should always hold the trigger in when gassing up. Let us know if it leaks with the trigger pulled.

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                    • gunangel
                      AGD Pride
                      • May 2005
                      • 285

                      #25
                      well it would leak with or without the trigger held down is what i meant. the reason this was so problematic for me is that I feel like I know mags. I run a pneumag so no sear arm etc to worry about, but i did check my sear and all and they all looked fine. for some reason the bolt would stay forward, not allowing the bolt to catch.

                      but...

                      i think switching to the rt on/off, replacing the spring, replacing the inner and outer carrier o-ring, and oiling everything might have done the trick. testing was technically inconclusive as the valve ate the rt on/off o-ring O_o (I had to fish it out of the little hole for the on/off pin in the valve swallowed a good 1/8 of the ring)...but it resets when i push it back with my finger now. ran out of air but hopefully that'll help you a bit.

                      thanks for all the advise so far. one final test to go!

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                      • warbeak2099
                        That is my foot!
                        • Jan 2004
                        • 4447

                        #26
                        I fixed half of the problem by turning the velocity up. The sear will now catch the bolt, but only when I push the bolt back manually. When I pull the trigger, the bolt still sticks forward and I have to push it back.
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                        • athomas
                          Of course it works-its AGD
                          • Jan 2002
                          • 8039

                          #27
                          I would check to see if the rail bushing is in place as mentioned by secretweaponevan
                          Except for the Automag in front, its usually the man behind the equipment that counts.

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                          • warbeak2099
                            That is my foot!
                            • Jan 2004
                            • 4447

                            #28
                            It is. I am quite sure right now that it's the on/off. I think there's something up with my ULT. I will have to test this after I get new o-rings for my stock RTP on/off.
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                            • secretweaponevan
                              Only HALF Polish!
                              • Sep 2007
                              • 1132

                              #29
                              Originally posted by warbeak2099
                              I fixed half of the problem by turning the velocity up. The sear will now catch the bolt, but only when I push the bolt back manually. When I pull the trigger, the bolt still sticks forward and I have to push it back.
                              First, when you hold the trigger in while gassing up, are there no leaks?

                              Second, how far forward does the bolt stick?
                              If it is all the way, it is probably an on/off problem.
                              If it just like 1/4" it is probably a carrier/spacer/shim issue.

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                              • gunangel
                                AGD Pride
                                • May 2005
                                • 285

                                #30
                                There is a constant leak it goes PSHHHHHHHH when you air it up, when you pull the trigger it is still going PSHHHHHHH when you let go of the trigger it is still going PSHHHHHH.

                                The bolt seems to be sitting halfway, just enough to put my finger in and reset it, now that it resets. During my fiddling I believe I also turned up the velocity. Strange tho, it worked perfectly fine with the same settings the game before and no o-rings were blown or worn upon inspection. I guess she's just finicky like that. Hopefully I'll know more with another fill.

                                I really appreciate all the help, and I am so glad someone had the same problem now at least I know my mag isn't the only one behaving badly .

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