Slow Reset

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  • BlackOps
    Registered User
    • Dec 2004
    • 122

    #1

    Slow Reset

    So I've converted another mag with E lowers. Replaced the ULT in the valve with the RT on/off with the emag pin and quad O-ring. It fires fine (per se) in both mechanical and electronic modes, but then it takes almost a full second for the on/off to reset. I can hear it hissing while its trying to reset until it finally clicks into place, and then it stops. I've replaced the quad o-ring, the one that that goes around that and the little one inside the on/off. Same effect. I did grab the on/off from my other emag and used it with quad/top oring on my new setup and it worked fine. Seems to me that maybe the pin is fit too snug in the inner oring? I had read in a few places where people had the same problem and it eventually wears in, so I spent 30 mins on the couch last night popping off shots to see if it would wear in, but I've had no luck.

    As is usually the case, I'm probably just over looking something simple.
  • Ando
    Magusmaximus
    • Jun 2009
    • 4144

    #2
    I have a mag that does that same crap, mine isn't a wear in problem. My fix was tightening the field strip screw a little over finger tight with a allen key.
    My Feedback

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    • BlackOps
      Registered User
      • Dec 2004
      • 122

      #3
      Yeah, no luck with that either. Maybe I'll order some O-rings and try a handful of different ones.

      Comment

      • Coralis
        Hyper Micro
        • Aug 2005
        • 1285

        #4
        try retuning your level 10 .... bolt stick can cause the same problem

        Comment

        • athomas
          Of course it works-its AGD
          • Jan 2002
          • 8039

          #5
          Yes, bolt stick. The vent hole is exposed during this time. Residual air is vented out the bolt stem vent hole until the pressure is low enough that the bolt spring can overcome both the oring friction and the force of the residual pressure. Once this happens, the bolt resets and the on-off pushes the sear forward to reset the trigger mechanism.
          Except for the Automag in front, its usually the man behind the equipment that counts.

          Comment

          • BlackOps
            Registered User
            • Dec 2004
            • 122

            #6
            If it was bolt stick, why does it work when I swap out on/off assemblies?

            Comment

            • Ando
              Magusmaximus
              • Jun 2009
              • 4144

              #7
              Measure the pin in that on/off and see if it's the correct size or try using a regular oring setup with the one giving you problems in the E-Mag. The quad isn't mandatory to use with lowers.
              My Feedback

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              • athomas
                Of course it works-its AGD
                • Jan 2002
                • 8039

                #8
                Sometimes just moving parts around temporarily fixes a problem. It isn't really a fix but works for now. If this is the case, the problem will return. Try swapping the on-off assemblies back and see if the problem comes back. That is one way to help find out.

                Check the length of the on-off pins.
                Except for the Automag in front, its usually the man behind the equipment that counts.

                Comment

                • BlackOps
                  Registered User
                  • Dec 2004
                  • 122

                  #9
                  The pin is a tad bit longer than I expected. Not much, its .7135.

                  I removed the quad o-ring and replaced it with the standard o-ring that normally goes in its place and everything seems to be working fine. Not sure that's the 'appropriate' fix, but its doing the job, which is what matters in the end.

                  Thanks again for all the fast responses and help.

                  Comment

                  • athomas
                    Of course it works-its AGD
                    • Jan 2002
                    • 8039

                    #10
                    That difference in pin length shouldn't matter. Are the body and rail standard retro/emag parts?
                    Except for the Automag in front, its usually the man behind the equipment that counts.

                    Comment

                    • BlackOps
                      Registered User
                      • Dec 2004
                      • 122

                      #11
                      Yeah, full size Tac One body and a wingless RT rail.

                      Comment

                      • Tunaman
                        Specialized AGD Tech

                        • Dec 2000
                        • 8643

                        #12
                        I just did a mag that I spent 3 hrs on...couldn't get it to work for beans. Same symptom as yours. Finally swapped the rail with a new one and the problem is gone.
                        Email me for low prices on ALL AGD Products and more. [email protected]
                        Tunamart

                        Comment

                        • athomas
                          Of course it works-its AGD
                          • Jan 2002
                          • 8039

                          #13
                          Interesting. Perhaps there were some rails that went through the system that were out of spec.
                          Except for the Automag in front, its usually the man behind the equipment that counts.

                          Comment

                          • Spider-TW
                            U R techno-literate!

                            • Oct 2006
                            • 3554

                            #14
                            Maybe the sear is rubbing on the sides of the rail? I had an old setup that had a good rub on the sear from the rail. I also had a rail that the sear pin had to be pressed all the way into the slot (am/mm), or else one side would sit a little high and the whole thing would bind. Then there's the homemade sear pins that aren't straight anyway.

                            Comment

                            • MingusX
                              Sweede
                              • Jul 2010
                              • 23

                              #15
                              make sure you have the rail bushing in place.

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