One for the Pros to venture forth on. XMT Body not getting into the rhythm.

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  • XtraKargo
    BPM AutoMagger
    • Apr 2013
    • 108

    #1

    One for the Pros to venture forth on. XMT Body not getting into the rhythm.

    Hey all,

    So I have recently gotten an XMT ULE with the Classic RT look, for an X-valve. When I had the Valve in the original AGD ULE body, it was a perfect, walkable, rhythm to the trigger. Once I dropped in the XMT Body, it catches on the return briefly. Then resets, and is able to fire again.

    SOOOOOO, I tried my classic valve from a Minimag. Shoots fantastic in the XMT Body. Then I had to test the X-Valve and finally gotten it back to perfection in the AGD ULE with no shims in the LVL10 using a 1 carrier, gold spring and lubing everything once again. I have the Thumb screw finger tight only (in the AGD ULE I would put the 1/4 turn on it) A mag whisperer once told me to try adjusting the Thumb screw slightly with different aftermarket parts. No luck here.

    So here is a short Video. And my open mind looking for insight. Thanks folks.

  • BigEvil
    www.BigEvilOnline.com

    • Feb 2005
    • 9333

    #2
    Do you have the correct front frame screw and rail bushing in there? Also, try tightening up the thumbscrew with an allen wrench.

    Comment

    • XtraKargo
      BPM AutoMagger
      • Apr 2013
      • 108

      #3
      Same screw that came from the AGD ULE body and the bushing is there as well.

      If I tighten the thumbscrew it is the same deal.

      (By the by - you were the Mag whisperer, thanks)

      Comment

      • need4reebs
        OutKasT 4 Sho!!!

        • Feb 2011
        • 1441

        #4
        with the body off the rail try dropping the bolt into the body to see if it will fit into the breech...you might have a bur somewhere around the breech...a lil needle file and a few minutes should take of that if you have a bur.
        http://i257.photobucket.com/albums/h...8715822556.gif

        Comment

        • XtraKargo
          BPM AutoMagger
          • Apr 2013
          • 108

          #5
          Originally posted by need4reebs
          with the body off the rail try dropping the bolt into the body to see if it will fit into the breech...you might have a bur somewhere around the breech...a lil needle file and a few minutes should take of that if you have a bur.
          Drops in clean. I even removed the detents during the video, they shown some where but the body is clean inside.

          Comment

          • nak81783
            Registered User
            • Nov 2001
            • 782

            #6
            When you say it catches on the return, do you literally mean the bolt is slow to spring back, or do you mean it just recharges slowly?

            If the distance from the center of the rear field strip screw to the bolt spring seat inside the body is different (it can vary significantly even from one AGD body to another), you may need to tune the Level 10 to that particular body. Perhaps the distance is longer, so you need a longer spring than the gold one you indicated you are using. Are you using the largest carrier that doesn't leak? If not, this hypothesis holds more water, as bolt stick with a weak spring (for the longer distance anyway) is more likely.

            Are you using a ULT? That may need to be tuned for a specific body as well. Slowly add shims to see if that helps.

            I haven't done a pneumag (yet). Is the ULT required to help it cycle at a lower lpr setting?
            Last of the Salzburg Clan

            Comment

            • XtraKargo
              BPM AutoMagger
              • Apr 2013
              • 108

              #7
              It is strange, it returns quickly, then pauses for a short period, and clicks into place.

              There isn't a ULT involved, but it is a pneumatic trigger. Very light trigger pull and easily walkable.

              I will double check my carrier to O-ring again for leaks. Just to be certain.

              Comment

              • BigEvil
                www.BigEvilOnline.com

                • Feb 2005
                • 9333

                #8
                Crank your velocity way up and keep firing it. See if it goes away after a while and then lower your velocity to normal. Ive seen similar issues on new Xmag breeches. You would see some wear on the inside where the bolt would rub slightly. Once you saw where it was rubbing, you could polish it out with some emery cloth.

                Comment

                • nak81783
                  Registered User
                  • Nov 2001
                  • 782

                  #9
                  What is the bottom wall thickness of the working vs. non-working bodies?

                  What length on/off pin are you using? If .750", humor me, and try a .712" if you have one.

                  Edit: I should say I don't expect the shorter pin to fix the issue, although if it does great. I would rather like to know if it gives a different result - barrel leak, bolt never resets, etc. On the rare chance that you have a .765" pin, try that one too, and let us know what it does.
                  Last edited by nak81783; 08-07-2013, 10:43 AM. Reason: Clarified pin request
                  Last of the Salzburg Clan

                  Comment

                  • nak81783
                    Registered User
                    • Nov 2001
                    • 782

                    #10
                    Originally posted by BigEvil
                    Crank your velocity way up and keep firing it. See if it goes away after a while and then lower your velocity to normal. Ive seen similar issues on new Xmag breeches. You would see some wear on the inside where the bolt would rub slightly. Once you saw where it was rubbing, you could polish it out with some emery cloth.
                    Would it be advantageous to do this with a Level 7, if available, to really beat things into submission?
                    Last of the Salzburg Clan

                    Comment

                    • XtraKargo
                      BPM AutoMagger
                      • Apr 2013
                      • 108

                      #11
                      Now I don't have a set of digital calipers, but my old ones show it as just shy 1/16th, and they both are the same, the calipers slides right off of one and onto the other. With the carrier I stepped up to 1.5 and it leaked so I went back to a 1. (granted this is a fresh o-ring to, in my troubleshooting on my own, I figured why not, to see what happens without shims and where I end up on carriers. really was good refresher on the LVL10 also.) I would venture to say this one is a .750 since it just touches the 3/4 mark. I will have to pull my Retro Valve out of storage to see if it is different or not.

                      With the Velocity turned all the way up it still sticks, and it appears to rub on the upper portion of the body where the outer rim of the bolt pushes against the top (that is the only part that looks scored, but mildly so, a darker grey color). The breech still looks clean. I wondered about the LVL7 myself, if it would make a difference.

                      Comment

                      • XtraKargo
                        BPM AutoMagger
                        • Apr 2013
                        • 108

                        #12
                        Also with that guy turned up it gets LOUD! HA

                        And just for good measure I tried the longer spring.



                        With the velocity turned up I blew out my foamy, so I will get the joy of replacing it later as well.
                        Last edited by XtraKargo; 08-07-2013, 11:42 AM.

                        Comment

                        • nak81783
                          Registered User
                          • Nov 2001
                          • 782

                          #13
                          Is the rubbing along the entire stroke, beginning only, end only?

                          Oh and to clarify, when you put your classic valve on the XMT body, was all that still the pneumag rig, or did you put the XMT body on a standard Mag?

                          I'll do some tinkering tonight to see if anything else comes to mind. Would still like to know what a different pin length does if you can find one.

                          I just blew my first foamie off (that I can remember) recently when tinkering with RT effect. Loctite Ultra Gel seems to be working well. Works well on the bumpers too. It's cheaper and easier to find than Loc-Tite 380 or IC-2000, but it has the same rubber toughened, impact resistance properties. I used a dental pick to scrape off the old adhesive. It snaps off in flakes. I also then scuffed up the parent metal and cleaned it with wifey's nail polish remover. Seems to be holding well.

                          Edit: My X-Mag and ULE bodies have rub marks inside the top of the body near the spring seat. Just an FYI, as the degree to which your marker is rubbing may be different.
                          Last edited by nak81783; 08-07-2013, 02:09 PM.
                          Last of the Salzburg Clan

                          Comment

                          • XtraKargo
                            BPM AutoMagger
                            • Apr 2013
                            • 108

                            #14
                            Originally posted by nak81783
                            I just blew my first foamie off (that I can remember) recently when tinkering with RT effect. Loctite Ultra Gel seems to be working well. Works well on the bumpers too. It's cheaper and easier to find than Loc-Tite 380 or IC-2000, but it has the same rubber toughened, impact resistance properties. I used a dental pick to scrape off the old adhesive. It snaps off in flakes. I also then scuffed up the parent metal and cleaned it with wifey's nail polish remover. Seems to be holding well.
                            Thanks for the tip!

                            I tried a Minimag rail and the XValve and got the same thing, but my most recent postings have been with the Pneumag setup.

                            I would guess it to be the end, or return it is scuffing, but this is minimal at best. It is only directly above the Sear Slot, and doesn't look roughed up. The detente with the smaller/thinner o-ring was fairly chewed up. This doesn't look like that.

                            Comment

                            • nak81783
                              Registered User
                              • Nov 2001
                              • 782

                              #15
                              So the problem follows the XMT body and X-Valve? Without those two together, everything works as it should? Am I understanding that correctly? Does the classic valve have a Level 7 or 10?

                              Also, when asked about the front frame screw, you said it's the same as the one you used on the ULE body. However, is it snug? If so, make sure the head is securing everything together. In other words, make sure it didn't bottom out, and the head isn't able to snug up to the trigger frame. If this is the case, put a washer between screw head and trigger frame, and see if that helps.
                              Last of the Salzburg Clan

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